Todays Project - What did you do today?
Hi Lads,
I am glad to report the mower is all done and been tested and is now nice and quiet steers better and cuts nice, not to mention the owner being very happy with her 'new' mower, I tested it to make sure all was well but she is now itching for the grass to grown even a touch so its a good enough excuse to get her revamped mower out lol.
Here is the rest of the job.

First all the top plates were tacked in place.

[Image: mowerrepair3001.jpg]

Then a new skirt , clamped and tacked into position .

[Image: mowerrepair3003.jpg]

Due to the old repair having a bar welded along the front with too much old snotty weld to grind off there ended up a section to be patched with a strip as the old skirt was about half an inch deeper than the new strip of metal I had to hand so this front area was patched in to replace the cut out section. The underside where the rot had been cut out was tacked to the new top and the areas filled with car body filler to seal them so grass would not pack between the two layers of plate.


[Image: mowerrepair3004.jpg]

The tacked seam between the top plates and the skirt was welded leaving alternate gaps then worked back around filling in the gaps to try to stop too much distorsion, this seemed to work as the whole thing stayed nice and flat to the floor.

[Image: mowerrepair3005.jpg]

Next I marked around the skirt with chalk on the floor and made a new bar to beef up the bottom of the skirt. I only has some 14mm black bar but in three short bits so by trial and error bent these bits in the vice to follow the chalk line then welded them together. Then welded them to the bottom of the new skirt.

[Image: mowerrepair3006.jpg]


[Image: mowerrepair3008.jpg]

The underside was undersealed then the blades , pulleys etc all built back up and the top side seam sealered around the welded areas.

[Image: mowerrepair3012.jpg]


[Image: mowerrepair3013.jpg]

One last hitch I noticed just in time to alter before painting , the return spring for the deck lowering lever was not a very good design so I managed to find a better spring in my scrap box and welded a strong washer for it to hook on to, this was a better spring and more secure way of fixing it than the original.

[Image: mowerrepair3015.jpg]

Next a coat of etch primer.

[Image: mowerrepair3016.jpg]

Then a few coats of a very dark grey satin finish that matched the rest of the dark bits on the tractor as I had no orange paint and would not have got a match for the original anyway as faded with age. The grey was darker than it looks here , it was hot sunny day so baked it dry in no time.

[Image: mowerrepair3017.jpg]

This it the finished job all back together, looking quite smart if I say so myself.

[Image: mowerrepair3020.jpg]


[Image: mowerrepair3019.jpg]


It should last a good few more years now and continue to give good service, my old friend is delighted , was nice to see her face when she saw it was not just a few horrible patches clagged on with sealer and snot weld like the last time the lawn mower dealer 'fixed' it lol.

Cheers Mick
Micktoon, proud to be a member of MetalworkingFun since Sep 2012.
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Cracking job
Very well documented as well DroolDrool
John
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Great rebuild Mick. The seam from the top to the skirt turned out real nice.
Free advice is worth exactly what you payed for it.
Greg
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I expected nothing but the best from you!

Do you think it weighs much more than the original? The better spring(s?) should negate any increase, while a more robust build like that won't likely ever fail.

Well done!
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Top job there Mick. I'd have not picked it as being anything other than factory after seeing it back on the mower. I bet the old girl has ducked off to the shops to by some fertilizer!
Hunting American dentists since 2015.
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Just a small project today

I had some inserts given to me so made a holder for them.

[Image: P1010304_zps6e306c47.jpg]

Welded a side Peace on and shaped the sides

[Image: P1010305_zps8425ed13.jpg]

[Image: P1010307_zps3e3f28da.jpg]

[Image: P1010308_zpsd45c7e05.jpg]

And the finished holder

[Image: P1010310_zps46ef6651.jpg]
mfletch, Try to do the best you can and that's good enough
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Nice going Fletch , just one wee thing ,you should have made the holder so that it supports the cutting edge right under the tip .

Here is my efforts ,,,,,,,is a flycutter I made a wile back .

[Image: P1060001_zps80667f6c.jpg]

[Image: P1060011_zps6df26b1e.jpg]

Even mine has a small unsupported area , one got a tad carried away with the file Blush , although TCT are hard they also can be quite brittle .


Just my two pence worth ,,,,,,,,,,,,,,keep up the good work Smile


Rob
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Mick, nice job on the lawn mower Thumbsup
Mfletch and Rob - a couple of very nice insert holders Thumbsup Thumbsup
Smiley-eatdrink004
DaveH
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Wow very good job Rob {nice} what mill do you have?

I agree and will build it up with weld and grind it back
mfletch, Try to do the best you can and that's good enough
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(07-24-2014, 01:49 PM)mfletch Wrote: Wow very good job Rob {nice} what mill do you have?

I agree and will build it up with weld and grind it back
Mfletch,
Just thinking this insert holder would have made a nice Project thread or a thread in the Lathe Tools. I'm just saying that's all Smile
Smiley-eatdrink004
DaveH
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